NOTICE: This
opinion is subject to formal revision before publication in the bound volumes of NLRB decisions. Readers are requested to notify the Executive
Secretary, National Labor Relations Board,
Forsyth Electrical Company, Inc. and Local
March 28, 2007
SUPPLEMENTAL DECISION AND ORDER
By Chairman Battista and Members Schaumber and
Kirsanow
On September 29, 2000, the National Labor Relations Board issued a Decision and Order in this case, affirming the finding of an administrative law judge that the Respondent violated Section 8(a)(3) and (1) of the Act by refusing to grant preferential reinstatement rights to three economic strikers after their unconditional offers to return to work.[1] The Board petitioned the United States Court of Appeals for the Fourth Circuit to enforce the Board’s Order. By unpublished opinion dated June 30, 2003, the court denied the Board’s petition, vacated its Order, and remanded the case for further explanation of the basis of its decision.[2] On December 9, 2003, the Board advised the parties of its decision to accept the court’s remand and invited the parties to file statements of position addressing issues raised by the court. Thereafter, the General Counsel filed a statement of position on remand.
The National Labor Relations Board has delegated its authority in this proceeding to a three-member panel.
We have reviewed the entire record in light of the court’s remand, which we accept as the law of the case. For the reasons that follow, we reverse the Board’s prior holding that the Respondent violated Section 8(a)(3) by denying reinstatement rights to former economic strikers David Jones, John Kimball, and Douglas Hill. We find merit in the Respondent’s argument that it lawfully refused to reinstate these individuals because, together with their discharged coworker Douglas Summers, they engaged in an unprotected work slowdown before going on strike. We shall therefore dismiss the complaint.[3]
i.
IBEW Local 342 (the
Summers, Jones, and Kimball worked at the Respondent’s Hamrick’s store jobsite, where the Respondent faced an intractable July 31 completion deadline. Much of the work at this and other ongoing jobsites involved the installation of overhead light fixtures. Several witnesses testified about productivity expectations for such work. Union Agent Maurice indicated that work variables made it difficult to provide specific numbers but, “in the best case scenario,” an electrician (journeyman/mechanic) should be able to install and wire a fixture in 5 minutes. He cited a Wal-Mart job where two people working together could complete 80-90 installations in a 10–12 hour workday under ideal conditions. Helper Larry Workman testified that he could install 30–50 lights in an 8-hour day, spending 15 minutes “tops” on each fixture. Respondent’s owner, Fred Benson, credibly testified that a team of five (Benson, Field Coordinator Ralph Holler, Office Manager Dave Hill, and two helpers) installed 300 light fixtures on one Saturday in July at Hamrick’s.
The Respondent hired Summers as a lead mechanic on the Hamrick’s job. Benson credibly testified that when Summers began work in June, this job was not behind schedule. However, according to Benson, Summers was “very unproductive.” On about July 7, Benson voiced concern to Field Coordinator Holler that “[t]hings [were] just not happening on that job. We’re getting fifteen (15) or twenty (20) light fixtures a day wired when there should be at least seventy (70) or eighty (80) a day per person. Outlets were not getting installed, wire was not being pulled, fixtures were not being terminated, contacts were not being mounted, floor work was not being done, conduits were put in the wrong space.” Summers himself testified that “[w]e wouldn’t maybe got about 10 or 15 lights [installed] in a day because I wouldn’t put myself in no strain.”
Benson considered replacing Summers when he hired Kimball. Instead, Summers took leave from work from July 14 to 24. He told Benson that he needed time off for a family emergency. In actuality, Maurice arranged for Summers to take a fully-paid training session as a union organizer during that time. When Summers returned to work, he was told that he was no longer needed because work at the Hamrick’s jobsite was substantially completed.
Jones testified that “between doing other things” he wired
9–10 lights a day at Hamrick’s. Helper Workman estimated that Jones spent a
couple of hours every day talking about the
Benson credibly testified that he checked Kimball’s job references and heard he was a “great mechanic,” but he proved to be unproductive on the job. According to Benson, Kimball “just really did not want to work. Didn’t want to work a full day. I had gotten, you know, a few light fixtures, six (6) or seven (7) light fixtures per day, just a total lack of concern for the completion of the job.” Kimball took 3 of his 7 days on the job to install 12–14 light fixtures in a dressing room, a task Benson estimated should have taken 2-1/2 to 3 hours.
Unlike the aforementioned covert salts, Hill worked at the
Respondent’s
On July 18, Kimball refused Field Coordinator Holler’s request to work voluntary overtime. On the next day, Kimball told Holler that he was going out on an unfair labor practice strike and to contact Maurice if Holler had any questions. Separately, Jones said the same thing to Benson. Accompanied at times by Maurice, Kimball and Jones picketed the Hamrick’s site and one or two other jobsites that day for a period variously estimated by witnesses as one-half to 4 hours.
On July 21, Maurice submitted a job application for himself that he had obtained in the previous week. Field Coordinator Holler accepted the application but said there were no jobs available. Maurice testified that he spoke successively to Holler and Benson. During these conversations, he offered to help the Respondent by providing union members for work. Benson indicated that he was not interested.
Although Hill complained to Benson about needing help, he
worked alone most days at the site until July 25. He then told Benson that he was going on
strike and to speak with Maurice about “any particulars.” After Hill went on strike, Benson discovered
numerous fixtures installed one-fourth to one-half inch off-center at
The Respondent did not hire anyone from July 20 until early August. Instead, Benson and other management officials worked nights and weekends to complete work at Hamrick’s and other jobsites. (The general contractor at one jobsite hired another electrical subcontractor to finish work there.) There were no exceptions to the judge’s findings that hiring was suspended because (1) as Benson credibly testified, he was too busy working on meeting job deadlines to review applications and conduct interviews, and (2) the recent productivity problems of individuals with good references and adequate experience showed that the Respondent’s “traditional means of verifying that a worker would be productive, by checking references, had broken down.” 332 NLRB at 820.
Jones offered to return to work on August 17. Office Manager Dave Hill told Jones there was no work available and “they didn’t see nothing coming up.” Jones spoke with Dave Hill again 2 or 3 days later. Dave Hill again said nothing was available. Striker Douglas Hill phoned Benson and offered to return to work on August 25. According to Hill, Benson “said that they only had one job going on at that time and he was thinking about laying off some men and he just didn’t need anyone at that particular time.” On November 10, Maurice sent Benson a letter announcing the end of the strike, conveying an offer by Kimball to return to work, and reiterating offers to return from the other former strikers. The Respondent did not reply to this letter.
It is undisputed that the Respondent did not replace the three strikers. Respondent finished work at four of the six jobsites by early August, thus, reducing its electrician staff needs to pre-June levels. Most employees hired by the Respondent from August 1995 through March 1996 worked in helper positions that were not substantially equivalent in pay and skill level to the former strikers’ mechanic jobs. However, after Jones and Hill offered to return to work, the Respondent rehired Jimmie Brewer on September 8 at mechanic-level wages. Brewer was rehired after being terminated for poor work performance. Benson testified that Brewer was originally hired as a mechanic, but he later decided Brewer was not capable as a mechanic. He was assigned helper work but his wages were not reduced.
ii.
The administrative law judge addressed allegations that
the Respondent violated Section 8(a)(3) and (1) of the Act by discharging Summers
and by failing to accord reinstatement rights to former economic strikers
Jones, Kimball, and Hill. At several
points in the judge’s decision, he discussed his conclusion that there was an unprotected
prestrike slowdown coordinated by Union Agent Maurice to pressure the
Respondent into hiring referred union members in order to meet pending job
deadlines: Forsyth I, 332 NLRB at 813–814, 817, 825–826. The judge determined
that Benson must have become aware that the slowdown was part of the
The judge found that the Respondent effectively discharged
Summers when it declined to assign him any further work on July 24. However, he concluded that the discharge was
lawfully based on Summers’ participation in the unprotected work slowdown. According to the judge, “Summers’ intent to
slow down the work, readily inferred from the circumstances, distinguishes him
from Jimmy Brewer, whom Benson described as a bad employee but rehired
anyway. The record does not indicate
that Brewer deliberately tried to produce little. His spirit was willing even if his
performance was weak.”
Although the judge’s slowdown analysis indicated participation
by Jones, Kimball, and Hill in this unprotected activity, he did not discuss
the Respondent’s contention that this deliberate conduct justified its refusal
to accord them reinstatement rights when they offered to return to work after
striking. Instead, the judge focused on
the alternative defense that their poor work performance prior to the strike, even if not part of a deliberate slowdown,
justified denying reinstatement. In this
context, the judge took a different view of the significance of Brewer’s rehiring
than for Summers’ discharge. He found
that the Respondent’s willingness to rehire Brewer in spite of past work
deficiencies undercut the assertion that the former strikers’ past lack of
productivity justified denying them reinstatement.
The Board affirmed the judge’s conclusion that the
Respondent’s refusal to reinstate the three former strikers violated Section
8(a)(3). It summarily affirmed the judge’s
rejection of the Respondent’s argument that the Respondent was justified in
denying reinstatement because they were unproductive.
On review, the Fourth Circuit held, inter alia, that the Board had provided an inadequate explanation for rejecting the judge’s findings relating to the slowdown. Noting that the judge had engaged in an extensive review of the record and a thorough analysis of this issue, the court directed the Board on remand to provide more than “conclusory assertions that the ALJ’s findings were without adequate support.” 69 Fed. Appx. at 168.[7]
iii.
It is well established that an employer violates Section
8(a)(3) and (1) of the Act by failing to reinstate a former economic striker
after an unconditional offer to return to work unless the employer can show a “legitimate
and substantial business justification” for its action. NLRB v.
Fleetwood Trailer Co., 389
As for the slowdown, the judge found that there was an unprotected slowdown prior to the strike, and that it was coordinated by Union Agent Maurice to pressure the Respondent into hiring union members. Indeed, the judge found that Summers’ participation in that slowdown was the reason for his lawful discharge.
The judge also specifically relied on credited evidence tying Summers, Hill, and Kimball to the slowdown: Summers’ testimony that he “wouldn’t put [him]self in no strain,” Benson’s testimony that Summers was very unproductive, Holler’s testimony about Hill’s lack of speed on the job, and Benson’s testimony that in spite of excellent references Kimball was very unproductive. We do not believe that this poor performance was simply the result of lack of skill or industry. Rather, we conclude that it was the result of a union-coordinated effort. In finding union coordination of the slowdown, the judge relied on evidence that all covert salt employees frequently communicated with Union Agent Maurice, Maurice further impeded progress on the Hamrick’s job by arranging for Kimball to take a week off in July, and each worker directed the Respondent to contact Maurice for details when declaring a strike.
Although not specifically mentioned by the judge, the
corroborative testimony about a comparable lack of effort by Jones on the
Hamrick’s job supports finding that he too participated in a deliberate work
slowdown. Concededly, Benson and other
witnesses for the Respondent may at times have overstated the number of daily
ceiling-light installations a mechanic/journeyman should be expected to perform. However, the number of installations
performed by Hill, Kimball, and Jones fell far short of even Maurice’s cautious
estimates for experienced journeymen.
Except for Hill, who credibly testified that he had a bad attitude and a
drinking problem at the time, there is no
apparent explanation for the slow pace of work other than that it was
intentional; and, as to Hill, notwithstanding other possible explanations, the
evidence still preponderates in favor of the intentional slowdown
explanation. Coupled with frequent
complaints from the covert salts about a need for more workers and pressure
from Maurice to hire union referrals, there is a reasonable linkage between the
slow pace of the work and the hiring objective ascribed to the
We next turn to the question of whether the Respondent
proved that the unprotected conduct was the reason it denied
reinstatement. We recognize that the
only reason the Respondent articulated in response to any of the offers to
return to work was that it no longer had any job openings for mechanics due to
the reduction in number of ongoing projects.[10] However, the failure to articulate a
particular reason for a decision does not itself establish that it is not
reason for the decision. As to the
reason for the decision herein, it is clear from Benson’s credible testimony
that he would not have reinstated any of the former strikers in any event because
of their prestrike activity, just as he would not offer Summers continued work
at another jobsite after July 24. Thus,
even though Benson and the Respondent’s other officials did not make the
explicit accusation that the poor performances were part of a deliberate work
slowdown, they correctly perceived the connection between this performance problem
and the
Further, credited testimony shows that the Respondent’s
officials and employees expressed concern among themselves prior to the strike that
Summers, Jones, Kimball, and Hill all performed far below expectations created
by their job experience and references.
This disparity between expectation and actual performance was one reason
Benson suspended hiring on about July 20.
Hill testified that Benson expressed an awareness of being targeted by the
In sum, we find that the Respondent has shown that the slowdown was the basis for its failure to reinstate Jones, Kimball, and Hill after they offered to return to work.[11] Their participation in an unprotected slowdown was a legitimate and substantial reason justifying the Respondent’s action.[12] Consequently, we shall dismiss the complaint’s sole remaining allegation that the refusal to reinstate Jones, Kimball, and Hill violated Section 8(a)(3) and (1).
ORDER
The complaint is dismissed.
Dated,
Robert J. Battista, Chairman
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Peter C. Schaumber, Member
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Peter N. Kirsanow Member
(seal) National
Labor Relations Board
[1]
332
[2]
[3] Inasmuch as we have found the Respondent lawfully denied reinstatement because Jones, Kimball, and Hill engaged in an unprotected prestrike work slowdown, we find no need to address other issues presented by the court’s remand.
[4] Unless otherwise stated, all subsequent dates are in 1995.
[5] At various times since 1991, Maurice had unsuccessful discussions with the Respondent’s owner, Fred Benson, about becoming a unionized employer.
[6] The Respondent also hired covert salts Ray Singleton and Bobby Lee Barnett. In Forsyth I, the Board affirmed the judge’s dismissal of allegations that the Respondent unlawfully failed to accord them striker reinstatement rights. The judge rejected the General Counsel’s claim that Singleton and Barnett were strikers, finding instead that each employee quit.
[7] We note that the General Counsel did not except to the judge’s slowdown finding. However, the Board implicitly construed the Respondent’s exceptions as requiring review of the factual support for this finding, and it reversed the judge on this point. While the court found the Board’s analysis inadequate, it did not challenge the Board’s scope of review.
[8] We also note that the General Counsel’s statement of position on remand from the court does not address the slowdown issue.
The Respondent’s unprotected work slowdown defense stands in
contrast to its defense that prestrike poor performance, even if not
deliberate, also justified denying Jones, Kimball, and Hill their reinstatement
rights. The judge correctly rejected
this defense. In general, prestrike work
deficiencies are not a legitimate and substantial business reason for refusing
to reinstate former economic strikers.
See TIC-The Industrial Co.,
320
[9] The Respondent alleges that Jones’ failure to groundwire fixtures and Hill’s off-center installation of fixtures were deliberate acts of sabotage in support of the work slowdown. The judge did not rely on this conduct in making his slowdown finding, and we find no need to pass on the sabotage allegation in affirming this finding.
[10] One of the issues presented for our consideration by the court’s remand is whether the Respondent proved it lawfully denied reinstatement for strikers because it no longer had job openings for them. As previously stated, we find no need to pass on this issue in light of our finding that the Respondent lawfully refused to accord reinstatement rights because the strikers had engaged in a deliberate prestrike work slowdown.
[11] The Respondent articulated this in its response to the charge. The response to the charge states, in relevant part, “Questions about whether the people named in your letter were legitimately on strike and questions about whether the serious misconduct they engaged in before the so called strike disqualified [them] from any future employment are serious and involve both legal and factual issues.” Further, the Board incorrectly stated in Forsyth I that the Respondent did not mention the slowdown at the time of the hearing. Respondent’s counsel did attempt to elicit testimony about a slowdown during his cross-examination of Maurice. As summarized above, Respondent’s witnesses also provided extensive testimony about an unexpected lack of productivity by covert salts that supports finding a deliberate, union-coordinated slowdown.
[12] As with Summer’s discharge, the Respondent’s rehiring of Brewer does not undermine the Respondent’s reliance on the prestrike lack of productivity when viewed as a deliberate slowdown. Brewer was a poor performer, but not intentionally so like Jones, Kimball, and Hill.